32-095 and 32-096 X-ray source control faulty capacitor – urgent!

Recently, I have seen the same problem on several 32-095 and 32-096 X-ray source controls which are used on older Physical Electronics PHI X-ray photo electron spectroscopy systems.

The issue is that C9, a 680 uF electrolytic capacitor blows out and the electrolytic material leaks out on the board.  Left unattended, the electrolytic etches and oxidizes the traces on the board.

If you have an older PHI XPS system that uses a 32-095 or 32-095 X-ray source control you should pull if out of the rack, remove the cover and inspect the board immediately.

If corrosion is present, then remove the board and remove C9.  Note the polarity of C9 as the + indicator on the board may be etched away.  Then, carefully clean the corrosion from the board as best as you can.   If in the shop I use some Alconox and let it sit on the board for a while, then rinse with DI water and let the board dry overnight.   In the field I have used isopropanol or methanol and cotton swabs.    Note that if the traces are corroded badly then they may come off the board as you clean it.  If so, you will need to use some fine copper wire to rebuild the traces.

Once the board is clean and dry, replace C9 with a new one.  I will dig into this issue some more and try to determine why this problem occurs so often and come up with a permanent solution.  In the meantime, I would recommend that the C9 capacitor be replaced every 5 years.

The pictures below show where C9 is located on the control board and what the corrosion looks like.

C9 removed
C9 location
C9 Neg towards connector

Low Cost Low Cost Molecular Sieve Trap

Update 5-28-23 – We tried this on two different pump set ups and it seemed to work well at first. But on one of the set ups the fine mesh O-ring became clogged with small Zeolite pieces and plugged up the line. We removed the Zeolite from that set up, the other one is working fine so far. It could be a function of the mesh size, we will continue to monitor set up #2.

Molecular sieve traps use zeolite pellets to adsorb water vapor, oil vapor and other gas molecules. They are particularly useful in preventing the back-streaming of oil vapor from the rotary vane pump into the turbo pump and vacuum chamber.

Molecular sieve oil mist trap

Molecular sieve traps are placed between the rotary vane backing pump and the turbo pump. Most molecular sieve traps also have built in heaters that are used to regenerate the zeolite once it becomes saturated with contaminants.

If you have an oil filled rotary vane pump, a molecular sieve trap is a must.  However, molecular sieve traps can be relatively expensive running from $500.00 to $1,000.00 or more depending on the size.

This blog post shows a way to use existing flexible metal hose to make a molecular sieve trap for a lot less.

The general idea is to fill an existing flexible metal hose which is connected between the roughing pump and the turbo pump with zeolite pellets.

Step one is to remove the flexible metal hose.

Next, insert a mesh screen centering ring on the end of the flexible metal hose that is closest to the roughing pump. Connect the flexible metal hose to the roughing pump.

I used this one from LDS – https://www.ldsvacuumshopper.com/nwstceri.html

The next step is to fill the flexible metal hose with Zeolite pellets.  I used these Zeolite pellets (also from LDS) – https://www.ldsvacuumshopper.com/mositrb1zepe.html

Once the flexible metal hose is filled completely (leave a little bit of room at the top) connect the flexible metal hose back to the turbo pump roughing port using another mesh screen centering ring.

Finally, label the flexible metal hose to indicate that the flexible metal hose is filled with Zeolite pellets.  

That way when the flexible metal hose is removed at some point in the future who ever removes it will know that they need to remove the top of the flexible metal hose first and to empty the Zeolite pellets before removing the flexible metal hose from the roughing pump.   You can also hold the bottom centering ring as the flexible metal hose is removed from the roughing pump. (That is one advantage that a regular sieve tap has is that the Zeolite pellets are contained and will not spill out when the sieve trap is removed from the backing pump).

In the experiment where I tried this idea the turbo pump and backing pump worked normally, there was no noticeable increase in the pumping time.   At some point in the future when the Zeolite needs to be baked out heating tape could be used.  Or the Zeolite pellets could just be replaced with new ones. Note that the volume of Zeolite pellets in the flexible metal hose is much less than what a regular sieve trap has, so the amount of adsorption would be reduced proportionally.  Even so I think that this is worth considering, especially in situations where there is no existing molecular sieve trap installed.

Total cost for the two mesh screen centering rings and the Zeolite pellets was under $90.00 Finally, if you are not familiar with LDS you should check them out.  They have a wide selection of vacuum related hardware at good prices and fun categories like REALLY Cheap Stuff and Surplus items.  https://www.ldsvacuumshopper.com/drypumps1.html

XPS analyzer control non-linearity problem

The 80-360 and 80-365/366 analyzer controls provide all the voltages to the 10-360 spherical capacitor analyzer that is used on many PHI (Physical Electronics) XPS systems.

80-365 boards Retard board is third from left

The retard voltage is used to slow down electrons and is essentially the sweep voltage.  In conjunction with the pass energy supply, the retard voltage controls the energy of the electrons that are being passed through the analyzer and into the electron multiplier and counting circuitry.

I recently had an interesting problem with a retard board on an 80-360 analyzer controller.  The issue was that the retard board output voltage was not linear.   Part of the calibration procedure for the retard board is to test the voltage at 11 specific voltages ranging from 253.6 volts to 1253.6 volts in increments of 100 volts.  This is a convenient way to confirm that the retard supply is linear.  The table below shows the hex commands that are used to set the voltages and the expected results.

In this particular case, the output voltages were close to correct at some points, but way off at other points as shown below. This non-linearity would present itself as inconsistent peak widths in the data as a function of kinetic energy.

These results at first glance look like a bit problem.  That is, the digital to analog convertor (DAC) voltages are likely off.  The DAC used in the retard board circuit is a 16 bit DAC and the output voltages should follow the voltages listed  below.

DAC Voltages

However, the DAC voltages were fine.  The retard voltage circuit comprises the DAC which drives a precision operational amplifier that in turn drives a high voltage switching supply.  Some precision high voltage resistors are  used to provide feedback.  The next most likely component that might be non-linear was the OP07 ultra-low offset operational amplifier (op amp).  The OP07 was replaced but did not solve the problem.

The next most likely cause of the non-linearity problem was the feedback resistors.  There is a total of 5 of these SX3730 5 watt wire wound high precision axial resistors in series.  To accurately measure those resistors, you need to lift one end off the circuit board.  Using my Fluke multimeter, I tested the resistance of each resistor and they all checked out as OK.  Ideally you will see very close to 1.0 megohms, but it might be off by .05 megohms. When a resistor is bad it will be open or be off by as much as .5 megohms. So, it seemed that the feedback resistors were OK as well.

That left not much in the circuit other than a few potentiometers. After spending some more time retesting all the components, I came to the conclusion that it had to be one of those feedback resistors. 

To test that theory I removed all 5 of the SX3730 1 megohm feedback resistors and replaced them with a single 5 meg ohm resistor.  And that worked!   So now I knew for sure that one of those 5 feedback resistors was the problem.  I measured the resistance of each resistor, and they looked OK.  But then I realized that the non-linearity is a function of the voltage applied to the resistor. At some voltages the resistance was OK, but at other voltages the resistance was off. 

I then decided to measure the resistance value again using a megohmmeter.  The model that I used was a Protek DI-2000M.  This megohmmeter (also called an insulation tester) puts 500 V across the resistor when measuring the resistance. I hoped that by putting 500V across the resistor that I would be able to see a greater difference in the resistance values. And that worked out as expected.  One of the resistors showed only 965 Kohms with the megohmmeter and 995 Kohms with the Fluke. I replaced that resistor and the calibration was perfect.  😊

In hindsight, duh. Since the gain of the circuit was changing as a function of the non-linearity of one resistor, the lesson is that when checking the resistance of suspected non-linear resistors, always use a megohmmeter since that will put much more voltage across the resistor than what a normal DVM will put out. Better yet, if possible, use the highest voltage that the resistor is rated for.

If your 80-360 or 80-365/366 analyzer control is not functioning properly and you need some help, please contact RBD Instruments for assistance as needed.